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A Method for Evaluating EMI/RFI Gasket Material
in PCMCIA Cards
David A. Case and Michael J. Oliver
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| Figure 1. The PCMCIA assembly was tested
at horizontal (pictured) and vertical polarizations.
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Evaluating the effectiveness of an RFI shielding
gasket is usually straightforward. One simply
tests the product with and without gasket material
installed and compares the shielding effectiveness
graphs or numeric profiles. If several types
of gasket materials are involved, you can repeat
the test for various combinations. This method
may be simple if you have a completed project.
But what if shielding effectiveness must be
determined before the electrical design is complete?
This was the problem confronting Instrument
Specialties Co. (Delaware Water Gap, PA) and
Aironet Wireless Communications (Fairlawn, OH).
The product in question was a 2.4-GHz spread
spectrum transmitter and radio fabricated on
a PCMCIA card form factor. Before the unit was
produced, it was necessary to determine what
gasket material was the best type to use prior
to the system being sonically welded together.
The solution was found
with an easily repeated test method to evaluate
the shielding gasket material. The preliminary
test method was based on a method used at the
now defunct ZDS EMC lab to evaluate electronic
cabinet designs. The big change was the physical
size of the unit, since we were attempting to
evaluate a PCMCIA card rather than a computer
cabinet. The final test configuration was a
modified MIL-STD-285 developed at Instrument
Specialties, using a test protocol developed
by Aironet.
The problem with performing
an evaluation of gasket material on a radio-based
product, or even a computer, is that temperature
variances and changes in the operating state
of the device can make repeatability difficult.
For example, duty cycles of the radio transmitter
and slight variations in power output over temperature
can change the test results. Even if the transmitter
has been modified to run at 100% duty cycle,
there are still enough other factors to add
additional uncertainty to your measurements.
Finally, when the transmitter is not yet designed,
how can you test the gasket material within
the frequency bandwidth of interest?
Our answer to this dilemma
was to design and fabricate a dipole antenna
on a PCMCIA card and install the PC antenna
into the PCMCIA shield. The card itself was
cut to match the size and outline of the planned
product. The antenna was milled out of the top
side of the board, leaving a conductive trace
around the outer edge. The back side of the
card incorporated a solid sheet of copper as
a ground plane. We tested two versions of the
card, one without a ground plane; we obtained
the best results with the ground plane.
As the radio design evolved, the PC antenna
card layout changed to match it. The 50-( )
cable (antenna lead) center conductor was soldered
to one side of the dipole and the cable shield
soldered to the other side and the ground plane;
an SMA connector was attached to the other end
of the cable. After many measurements and setup
configurations, it became clear that soldering
the cable shield to the ground plane on the
back of the antenna card was an important step
in achieving accurate and repeatable data. It
was very important to make sure that the ground
connection was well established on the ground
plane under the dipole antenna. If this ground
plane was left floating (no electrical potential),
or had a poor electrical connection, there would
be no difference between measurements with or
without a shielding gasket. This effect is caused
by radiated energy coupling to the bottom lid
of the PCMCIA card housing and radiating as
an antenna element due to near-field effects.
Adding a small ferrite core at the connector
end near the PCMCIA card lid helped reduce unwanted
emissions radiating from the coax cable. To
avoid unwanted emissions, low-loss cables (greater
than 90 dB isolation) connected the generator
to the spectrum analyzer.
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| Figure 2. Left-side setup for each
polarization. |
Figure 3. The signal generator and
spectrum analyzer. |
A fixture was designed and fabricated to retain
the PCMCIA card assembly (antenna, gasket, and
lids) and to establish repeatable compression
of the gasket configuration when under test.
We tested the assembly at horizontal and vertical
polarizations (Figure 1), with left side, right
side, and front setups for each polarization
(Figure 2). To establish an initial reference
level, the dipole antenna was tested without
top and bottom lids. The signal generator (transmitter)
and spectrum analyzer (receiver) are shown in
Figure 3.
To evaluate shielding gasket material, a control
(in this case, reference level minus the PCMCIA
card without a shielding gasket) must be compared
with the test specimen (reference level minus
the PCMCIA card with a shielding gasket). This
experiment determines whether the gasket material
is providing the required shielding effectiveness.
Thus, the total shielding effectiveness (dB) of
the test specimen is determined by a reference
level (dBm) minus the test level (dBm) when the
gasket is in place.
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| Figure 4. The dipole antenna elements
were insulated from the shielding gasket with
plastic tape. |
Figure 5. Ferrite and conductive tape
shielded open areas of the PCMCIA card housing.
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The dipole antenna is shown in Figure 4. The
dipole antenna elements were insulated from the
shielding gasket with plastic tape. The electrical
contacts of the dipole antenna at the base of
the antenna card were insulated from shorting
to the top lid with plastic tape. The tested unit
included ferrite around the antenna lead and conductive
tape on the back and front sides to shield open
connector areas of the PCMCIA card housing, as
shown in Figure 5. By loading the receiving cable
with a 50-( ) load, and transmitting at a
power level of 10 dBm, ground-floor noise levels
were recorded per the test bandwidth of 30 MHz
to 1000 MHz. Calibrated instrumentation was used
in measuring all test parameters.
The dynamic range of the test system configuration
(maximum output in dBm minus noise floor level)
was established at approximately 120 dB. The antenna
card without lids was tested and its response
zeroed out, and identified as 0 dB shielding,
as shown in Figures 69. The system was tested
at predetermined test points from 30 MHz to 1
GHz. (Though our main concern was digital emissions,
we also looked from 1 to 3 GHz to determine shielding
effectiveness at the receiver's local oscillators
and transmit frequencies.)
The characteristic shielding properties for
the molded-in-place gasket performed well
in comparison to the extruded gasket. For
all test positions and polarizations, the
molded-in-place gasket provided an average
of 20 dB more shielding from 180 to 280 MHz
and 600 to 1000 MHz. At the remaining frequencies,
30 to 155 MHz and 300 to 550 MHz, the gaskets
performed relatively the same, with each signature
trace interweaving.
At 900 to 1000 MHz the extruded gasket tends
to be equal to or less in shielding effectiveness
than the configuration with lids but no gasket.
This low-shielding characteristic from 900
to 1000 MHz was not exhibited by the molded-in-place
gasket. Instead, it showed an increase in
shielding of about 20 to 30 dB. This result
is due to superior electrical contact with
the PCMCIA lids of the molded-in-place gasket
compared to that of the extruded gasket.
In summary, the molded-in-place gasket provided
an average of 20 dB higher shielding effectiveness
than the extruded gasket for various frequency
ranges and test positions within 30 to 1000
MHz. The extruded gasket averaged approximately
15 dB in shielding effectiveness at various
frequency ranges and test positions compared
to the configuration with no gasket.
After evaluating the gasket material, our
next step was to see how it compared in a
real-world test with production samples. A
series of radiated tests for Class B compliance
were conducted at 3m at a couple of test sites.
For this testing, the radio was analyzed with
a laptop computer on an extender card, eliminating
any shielding benefits the laptop computer
could have provided. Results showed that the
radio without gasket material had the worst
profilein fact, it was out of FCC Class
B at several frequencies. The radio with the
extruded gasket material had about a 10 dB
improvement in the profile across the board
and readily met FCC Class B. When the over-molded
gasket was compared to the extruded gasket,
we saw again about a 715-dB improvement
over the extruded gasket (below 1GHz). These
results were very similar to what we saw when
we tested the test board with the various
materials, and they helped prove out the test
method. Despite some minor differences, the
method worked, providing useful engineering
design data.
This same test method can be used for evaluating
system cabinets. One would need to make the
antenna on a board roughly the same dimensions
as the system motherboard, or whatever the
suspected emittor of RF noise. Additional
thought on making a better match for the antenna
may help improve results. (For the next round
of testing, the plan will call for the coax
to be terminated by 50 ( ) before connecting
to the antenna to help reduce mismatch.)
Our best recommendation
is to try laying out all the parameters before
you begin testing. Although the method is far
from quick (at the start), it can provide a
repeatable baseline if done correctly.
David
A. Case, NCE, is the senior compliance and
reliability engineer responsible for worldwide
product approval at Aironet Wireless Communications
Inc. (Akron, OH), a firm with expertise in
spread spectrum technology. His responsibilities
include radio type approvals, as well as EMC
design and safety approvals for spread spectrumbased
products. He also handles product reliability
studies, EOS/ESD evaluation, and antenna and
power supply evaluation for WLAN systems.
Case is NARTE-certified in the fields of telecommunications
and EMC and ESD control, and he currently
chairs the IEEE EMC Society Representative
Advisory Committee. He can be contacted by
e-mail at dcase@aironet.com.
Michael J.
Oliver is a product development electrical engineer
at Instrument Specialties Company, Inc. (Delaware
Water Gap, PA). His responsibilities include electromagnetic
shielding development, project management, and testing.
Oliver has expertise in EMC shielding technology
with a background in military shelter electrical
systems and high-power antenna/radome design. He
currently serves as vice chairman of the ASTM D09.12.14
Electromagnetic Interference Subcommittee, as a
member of the Executive Committee for the SAE AE4
Electromagnetic Compatibility Committee, and as
a member of the IEEE EMC Society. He can be contacted
by e-mail at mike_oliver@instr.com.
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